This paper reports the detailed measurement of the film cooling effectiveness for a scaled up film-cooling hole with an expanded exit fed by a smooth and ribbed secondary flow channel, which is an arrangement typical of turbine blades. The experiments are carried out at blowing ratios ranging from 0.4 to 1.25, and ten different rib patterns, including forward oriented ribs and inverse oriented ribs, are evaluated. Furthermore, in order to develop an efficient film-cooling technique, several kinds of bumps are installed downstream of the hole exits and the effects of the bumps on the film cooling effectiveness are investigated. The bump structures tested here are semicircular, hemispherical, and cylindrical bumps. The results show that the rib orientation strongly affects the film cooling effectiveness. When the blowing ratio is comparatively low, the forward oriented ribs afford a higher film cooling effectiveness. On the contrary, when the blowing ratio is comparatively high, the inverse oriented ribs afford a higher film cooling effectiveness. The cylindrical bump provides a better spreading of the ejected secondary flow than the other bumps, leading to a higher film cooling effectiveness. To clarify how the bumps improve the film cooling effectiveness, computational simulations are performed. The simulations indicate that a longitudinal vortex, formed at the trailing edge of the cylindrical bump, improves the film cooling effectiveness by generating downward velocity vectors.
Skip Nav Destination
Article navigation
Research-Article
Experimental Study on Effects of Internal Ribs and Rear Bumps on Film Cooling Effectiveness
Eiji Sakai,
Toshihiko Takahashi,
Yukiko Agata
Yukiko Agata
e-mail: agata@criepi.denken.or.jp
Central Research Institute of Electric
Power Industry
, Japan
,2-6-1 Nagasaka, Yokosuka-shi
,Kanagawa-ken 240-0196
, Japan
Search for other works by this author on:
Eiji Sakai
e-mail: e-sakai@criepi.denken.or.jp
Toshihiko Takahashi
e-mail: tosihiko@criepi.denken.or.jp
Yukiko Agata
e-mail: agata@criepi.denken.or.jp
Central Research Institute of Electric
Power Industry
, Japan
,2-6-1 Nagasaka, Yokosuka-shi
,Kanagawa-ken 240-0196
, Japan
Contributed by the International Gas Turbine Institute (IGTI) of ASME for publication in the Journal of Turbomachinery. Manuscript received July 2, 2012; final manuscript received July 29, 2012; published online March 25, 2013. Editor: David Wisler.
J. Turbomach. May 2013, 135(3): 031025 (14 pages)
Published Online: March 25, 2013
Article history
Received:
July 2, 2012
Revision Received:
July 29, 2012
Citation
Sakai, E., Takahashi, T., and Agata, Y. (March 25, 2013). "Experimental Study on Effects of Internal Ribs and Rear Bumps on Film Cooling Effectiveness." ASME. J. Turbomach. May 2013; 135(3): 031025. https://doi.org/10.1115/1.4007546
Download citation file:
Get Email Alerts
Related Articles
An Energy-Based Method for Predicting the Additive Effect of Multiple Film Cooling Rows
J. Eng. Gas Turbines Power (December,2015)
Optimal Turbulent Schmidt Number for RANS Modeling of Trailing Edge Slot Film Cooling
J. Eng. Gas Turbines Power (July,2015)
Combined Effects of Freestream Pressure Gradient and Density Ratio on the Film Cooling Effectiveness of Round and Shaped Holes on a Flat Plate
J. Turbomach (April,2017)
Reverse-Pass Cooling Systems for Improved Performance
J. Turbomach (November,2014)
Related Proceedings Papers
Related Chapters
Modeling and Analysis of Flow Field in Intake Pipeline
International Conference on Control Engineering and Mechanical Design (CEMD 2017)
Saturated Boiling with Forced Flow
Two-Phase Heat Transfer
Critical Heat Flux in Flow Boiling
Two-Phase Heat Transfer